Cation Removal from Drag out Baths The Netherlands - Full scale

MANUFACTURE OF FABRICATED METAL PRODUCTS # 40

Background

This case study illustrates use of a cation exchanger for continuous cleaning of drag-out baths followed by evaporation in order to facilitates water reuse.

Cleaner Production Principle

Process modification; Recovery, Reuse and Recycle

Cleaner Production Application

This technique involves use of a cation exchanger for continuous cleaning of drag-out baths and evaporation followed by water reuse.

The plant operates a three-step cascade rinse behind the plating baths and the water is used to replenish the water evaporating from the process baths. This is supplemented with demineralized water. In the original process, a final rinse with tap water occurred after the cascade.

Because of a build-up of undesired cations such as iron, copper, and nickel in the process baths, drag-out baths are now treated over a cation resin. The water of the final rinse has been substituted with demineralized water and is also treated over the resin. The process liquor is difficult to be treated. By using the waste heat of the cooling system and controlling the process bath temperature, an extra amount of water is evaporated. The resulting wastewater is still treated in a DND installation. Lifetime of the untreated baths was about five years with the original process.

In the original process, the starting power was 10 V and 15,000 Amp. The voltage increased at a rate of 1 V/A. Due to limitations in the transformers, this meant that after about five years the process baths had to be thrown away. In the current situation, the voltage increased two volts in five years of operation, and then remained stable.

 Environmental and Economic Benefits

The process modification resulted in decreases in

Sludge production from 10 tons to 0.4 tons in five years.
Tap water consumption from 1330 to 15 m3/yr and demineralized water consumption went up 1320 m3/yr.
Energy consumption decreased from 99 MWH/yr to 59 MWH/yr corresponding to a saving of more than 40%.
The consumption of chromic acid decreased by 2,000 liters/yr.
Chemicals for the DND installation decreased from 2,000 to 20 liters/yr.
No adverse effects on product quality were reported in the source document. Instead, the quality should have improved since foreign elements have been removed.

The following are savings were realized using the modified process:

Savings in Dfl/yr
Less chromic acid 3000
DND treatment chemicals 8000
Waste disposal 700
Power consumption 5340
Tap water 1900

Operational and maintenance costs for the five year period are as follows:

  Old Process (Dfl) New Technology (Dfl)
New chromic acid 15,000 --
Waste disposal 3,500 140
Chemicals for DND 40,000 400
Power loss 74,250 44,550
Tap water 8,600 100
Extra demineralized water -- 33,000
Sewage costs 9,550 100

Costs over five years have decreased by Dfl 71,710. The payback period cannot be calculated due to incompleteness of investment data. However, based on the cost information given and the cost of an ion exchanger, it can be estimated that the payback period would be less than one year.

Constraints

No information was provided.

Contacts

Jan Ros, RIVM, Dept. LAE, Anthonie van Leeuwenhoeklaan 1, Postbus 1, 3720 BA Bilthoven, the Netherlands.
 
Name and Location of Company
Koni BV
Langeweg 1
Oud-Beyerland
Netherlands
Tel: 31-1860-12500
 
H. van Zessen
H.W. du Mortier
VOM
Jan van Eycklaan 2
Postbus 120
3720 AC Bilthoven
The Netherlands
Tel : 31-30-287111; Fax : 31-30-287674

Review Status

This case study was originally compiled by the UNEP IE Working Group on Metal Finishing. It underwent a UNEP IE funded technical review in 1994 for quality and completeness. It was edited for the ICPIC diskette in July 1995.

Subsequently the case study has undergone another technical review by Dr Prasad Modak at Environmental Management Centre, Mumbai, India, in September 1998.